Hello all,
I'm looking for a bit of input on this build; here is the history.
Initially, I was impressed with Paul's pebble
rocket mass heater series which was supposed to be "temporary" in nature such it could be torn down and rebuilt elsewhere. I scoured the forums and purchased the DVD series and looked at Ernie and Erica's book for details. I probably spent close to 6 months reading up on the how to's on rocket mass
heaters before attempting to actually build one.
The nature of the experiment demanded a six inch system and since weight was a factor I purchased a set of plans from Matt Walker for his ceramic
RMH core build. I figured no sense in redesigning the wheel. Below are the pictures (see attachments) I've taken of the build. The ceramic board was one inch thick and rated at 2300 degrees per board . This design call for two inches of ceramic board everywhere except the
feed tube where 1/2 split bricks were used to avoid wear and tear from the
wood.
see 1-MW-build 1
2-MW-build 2
3-MW-biuld 3
When I dry stacked the core, at this stage the riser was 24 inches tall. A this point I tested the core with a first burn.
The burn tunnel temp reached approximately 1400 degree in this build. I thought I could do better, and after reading that the higher the riser the better the draft, I took the rise to 39 inches and ran another test burn. (the only change made was the riser height)
This time the burn tunnel temp hit 1900 degrees and I had flame coming out of the riser. Not wanting to exceed the insulating factor of the ceramic board I figured this would be the design stop point. Inspecting the plywood underneath both layers of ceramic board revealed charring but the charring did not extend to the other side of the plywood. That was cause for concern as apparently the temp further up the burn tunnel exceeded the 1900 I measured at the tunnel opening. To compensate for this issue I laid a 1.25 inch granite pad immediately under the second layer of ceramic board. This seems to have resolved this issue.
At this point I deemed the core design a success and proceeded to begin the inside build.
As a small aside, it
should be stated that Matt Walker in one of his videos said he used aluminum foil to protect the ceramic board of the riser. I opted for this approach in my initial build inside.
The core foundation consisted of 1. 3/4 in plywood lined with aluminum tin foil, next 1.25 inch granite pad, next 1 inch ceramic fiber board rated at 2300 degrees.
see 4-core-foundation
Then the core build out. Version 1 of the firebox was built using 1" ceramic fiber board, with the feed tube using 1/2 brick splits. the feed tube was 4.5 x4.5, the riser internal dimension was 5"x5" for a CSA of 25. Six inch duct has a CSA of 30. So based on the math I figured the system was sound.
see 5-core-build
The riser was 39" tall made out of 1 inch fiber board. I reinforced the base with another round of fiber board and surrounded the base with firebrick. I wrapped the riser in three layers of tin foil per matt walker.
see 6-riser build v1
7-riser v1 final
After reading that moving the firebox a bit off center in the direction you wanted the heat to radiate, I moved the firebox 3 inches off center in the direction of the feed tube. Its true, you will get more heat radiated out in a specific direction by doing that.
Since this experiment is not necessarily predicated on permies low tech preferences, my first attempt at sealing things up was to use refractory cement. This proved a dismal failure, as cracks appeared even before it dried completely. My next option and much better solution was to use high heat silicon, rated at 600 degrees. Since the exhaust gas temp is not supposed to be that high at this stage of the drum I went for it. It works wonderfully well.
See 8-high temp silicon
For the mass ducting, I used 6 inch single wall piping and referenced Ernie and Erica's book for rise over distance and went a bit more using 1/2 inch over 10 feet for version 1. The design called for 2 ten feet runs which were tied into the chimney which consists of 3, 4 foot runs , 1, 90 degree elbow and 2, 45 degree elbows to get outside. I saw this solution at Paul's place when he built the pebble mass heater in his home. While he had an 8 inch system, I copied it for my 6 inch system. The Jury is still out on whether that was sound or not.
See 9-mass ducting v1
With the ducting cabled up and sealed I ran my first indoor burn. At this point, I thought I had solved the riddle. The top of the drum reached 1200 degrees and had a cherry red spot just above where you'd expect the heat riser to be located. A check outside revealed steam exiting the chimney.
The only down side and I knew this would happen going in, is, you really have to tend the wood feed on a
RMH. Every 20 minutes I had to add wood to the feed. This heater really ran through it.
Sadly this is where the story takes a dismal turn. This was the only time I achieved these results. Every subsequent burn thereafter was less and less effective until finally on about the 6-8th burn it started back blowing smoke and fire out the feed tube. For a system with effectively no moving parts, initially I was not overly concerned. Annoyed yes, to be sure, but I was pretty certain I could figure it out. (*dare to dream lol)
So, i popped the top drum off and discovered that the riser had pretty much fallen apart. The aluminum foil had disintegrated and the ceramic board had warped
enough to break the refractory cement seal around the board borders. Another thing I noticed was that the ceramic board that made the fire box tunnel was not holding up as well as I'd hoped.
So, I rebuilt the firebox using #2 refractory tile cut to the size and specs of the ceramic board parts, and rebuilt the riser using 1/2 split brick cut to size, and insulated the brick with the ceramic board.
see 10-core v2
11-core v3 pt2
12-riser v2
13-riser v2 insulatred
I rebuilt the riser out of 1/2 split firebrick per Ernie and Erica's recommendation in their book (except I cut the bricks to size) and put everything back together.
At this point I mention the CSA measurements in inches
The feed tube is 4.5x4.5 = 20.25
the riser internal is 5x5 = 25
the 6 inch duct has a csa of 30
I figured that made the system solid.
Additionally before placing the drum back on, I put 2x4s over the riser and measured the gap between the two drum sections. I got 1.25 inches. Since the 2x4s are 1.5x3.5 that would give me 2.25 inches of space between the riser and the top of the drum.
This time during the burn I had to close off 50% of the feed tube to get any draft and when the drum hit 400 degrees it flamed out and I got smoke blow back and fire out the feed tube.
I sealed off the feed tube with bricks and let it die out.
About this time, it occurred to me that maybe my mass duct really didn't have enough rise, so I tore that apart and reinstalled it with a 3 inch rise in each 10 foot section with a 1 inch rise between the end elbows for a total of 7 inches of rise before it hits the chimney. And I had the same issue as before: at 350-400 smoke blow back made its appearance.
In the meantime I met a young gentleman at one of the
local fireplace shops who had attended one of Paul's RMH Seminars, and explained to him the problems I was having and showed him my photos. He offered his opinion that the CSA of the exit duct going to the Mass was probably not enough. So, back to the
books and sure enough there is a 3 inch CSA requirement there I had totally overlooked (much to my chagrin).
I tore out the back of the support bricks and again cut them to the size I needed and also considered since the surfaces of the ceramic board, the tiles and the firebricks that support the riser were not perfectly smooth, I would put a thin (1/2 inch) layer of
cob between the riser and the core to make sure everything was sealed up tight.
This having been about the fourth time I had torn things apart, another thing became apparent. While the silicone is wonderfully easy to apply and does seal things up, its a real pain in the rear to get off and clean up. So, this time since I was cobbing things up, I decided to use cob for the resealing of the drum.
see 15-sealed by cob
16-exit duct csa
With the new duct gap in place and everything rebuilt, the final burn was more dismal than any of the others such that even a small fire to start came back through the feed tube.
So this is where I currently sit. There has to be a choke point somewhere, and having just read the post on how to make your RMH rockier, the only other think I can think of is to lower the riser, or move the whole thing back the the three inches I moved it forward.
While I'm not freezing, as the propane back up is in place, my pocket book is hemorrhaging to keep the propane flowing. So the sooner I can fix this the sooner my pocketbook will love me again lol.
Thanks in advance for your posts and constructive comments.
Jim
PS I did attempt to upload the movies of the test burns but the forum wasn't having any of that. Sorry. Is there a solution?